pneumatic_ip_report
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pneumatic_ip_report [2016/02/21 22:23] – joaomatos | pneumatic_ip_report [2016/03/13 00:47] (current) – joaomatos | ||
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- | **WEEK 01 ** | + | ** WEEK 01 ** |
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- | I will already post what i finish on the [[pneumatic_ip_tutorial|tutorial page.]]= | + | I will already post what i finish on the [[pneumatic_ip_tutorial|tutorial page.]] |
*Overview : how the system works. | *Overview : how the system works. | ||
*Transfer Function Derivation . | *Transfer Function Derivation . | ||
*Control Method (PD). | *Control Method (PD). | ||
*Estimating Gains Using LQR. | *Estimating Gains Using LQR. | ||
+ | |||
+ | ---- | ||
+ | |||
+ | |||
+ | ** WEEK 02 ** | ||
+ | |||
+ | *Started to sketch the assembly when all the parts got in the lab.I had some trouble in what to use for the pendulum ( the pendulum from the original project was not on the lab). Once i got the pendulum ( 1/2in steel bar ) i had to figure out a way to fix the bar into the rotational encoder ( i'm waiting a friend print a support on a 3d printer for me ). | ||
+ | *Started to build the circuit. | ||
+ | |||
+ | ---- | ||
+ | |||
+ | |||
+ | |||
+ | ** WEEK 03 ** | ||
+ | |||
+ | *Assembled the model on the wood | ||
+ | *Tested the encoders connection with the arduino and the readings. | ||
+ | *Tested the DAC and the Arduino Connection - digital input have to give the exact desired voltage output at the operational amplifier. | ||
+ | *Started to post the tutorial steps. | ||
+ | |||
+ | ** PROBLEMS ON WEEK 3 ** | ||
+ | |||
+ | **Fixing the rotational encoder on the cart:** I'm having trouble in how to fix the rotational encoder into the cart (I'm using the cart from the original project , but the rotational encoder that came in the same box of the other parts is not the same from the tutorial ( I have the s5 sensor , with bearing (it does not fit on the hole of the cart ). | ||
+ | |||
+ | **Voltage output at the proportional valve:** I'm having trouble on the voltage output.Even if i change the digital value on the arduino code , the voltage at the proportional valve still at 8,4 V (it is expected the voltage to change from 0 to 10V when changing the digital input value at the arduino code). I rebuilt the circuit changing the operational AMP , DAC and all the resistances, | ||
+ | |||
+ | ---- | ||
+ | |||
+ | |||
+ | ** NEXT STEPS ** | ||
+ | |||
+ | To finish all the building: | ||
+ | |||
+ | *Fix the voltage at the proportional valve problem. | ||
+ | *Figure out a way to fix the sensor into the original cart. | ||
+ | |||
+ | And after: | ||
+ | |||
+ | *Adjust the gains on the arduino code until the balance is good enough | ||
+ | |||
+ | |||
+ | ---- | ||
+ | |||
+ | ** WEEK 04 ** | ||
+ | |||
+ | *The problem of the voltage at the proportional valve was solved. | ||
+ | |||
+ | {{youtube> | ||
+ | *The connector that i printed broke and i will print another one. | ||
+ | |||
+ | {{:: | ||
+ | |||
+ |
pneumatic_ip_report.1456122231.txt.gz · Last modified: by joaomatos